Rudder Repairs

 

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1

Rudder_post_thruhull.JPG (61107 bytes) Rudder_post_thruhull_1.JPG (55111 bytes) Broken_rudder_stud.JPG (37590 bytes) Rudder_post_before_work_begins.JPG (73395 bytes) Rudder_post_housing_studs.JPG (45086 bytes)

Here's the original problem, a stud has corroded through that is used to bond the rudder to the prop shaft. The problem was worse than we thought and all the studs had problems with corrosion. It had been 20 years or so since the stuffing box had been installed and even with all the nuts off, everything was still tight.

2

Rudder_post_locking_key_1.JPG (32304 bytes) Rudder_post_locking_key_2.JPG (44612 bytes)

Next job was to get the locking key out of the slot on the rudder post. I would swear to the fact they had welded it in! We tried pounding. We sprayed it with every conceivable 'loosen-em-up-mouse-milk' made. We heated it. We cooled it. We drilled it. And then we pounded it some more. Finally we drilled it again, put the torch to it and pounded away with a chisel and sledge hammer. It budged, slightly. More torch, more pounding and it started giving.

3

Rudder_locking_key.JPG (53956 bytes) Rudder_locking_key_1.JPG (55097 bytes) Rudder_locking_key_2.JPG (45505 bytes) Rudder_post_housing.JPG (49599 bytes) Rudder_locking_key_slot.JPG (75360 bytes)

With the key out at last (this was a several hours job over a 3 day period), we were able to remove the cap off the stuffing box. Well this wasn't too bad and only took about 20 minutes of pounding, spraying and prying to loosen it. Now we expect to lift the stuffing box off the rudder post. Guess again.

4

Rudder_stuffing_box_finally_off.JPG (68161 bytes) Rudder_post_and_housing.JPG (90562 bytes) Rudder_stuffing_box.JPG (77088 bytes) Rudder_post_thruhull_pipe.JPG (36231 bytes) Rudder_stuffing_box_1.JPG (67781 bytes) Rudder_stuffing_box_bottom.JPG (44092 bytes) Rudder_stuffing_box_top_flange_1.JPG (74739 bytes) Rudder_stuffing_box_top_flange_2.JPG (77648 bytes)

The way my brain works is if you have studs mounting into the hull, the fitting (in this case the stuffing box) should lift straight up off the studs. I guess they think differently in New Zealand. After much pounding and prying, the stuffing box came up about 1/2" and refused to come up any more. It would twist from side to side as much as the studs would allow, but no higher up the rudder shaft. At this point I used a cutting wheel on the dremel and cut the studs off at the fiberglass. The stuffing box unscrewed off a small pipe and came off the rudder post. They may have used studs, but it's going back on with lag bolts.

5

Port_side_of_rudder.JPG (35089 bytes) Rudder_shoe_-_port.JPG (67557 bytes) Starboard_side_of_rudder.JPG (35011 bytes) Rudder_shoe_-_starboard.JPG (69107 bytes)

Now we had to drop the rudder. First job was to support the bottom of the rudder and remove the rudder shoe.

6

Wire_brushing_rivets.JPG (47710 bytes) Rivets_after_wire_brushing_1.JPG (62449 bytes) Rivets_after_wire_brushing_2.JPG (74364 bytes)

Then wired brush the old paint off the heads of the rivets.

7

Grinding rivets2.JPG (60898 bytes) Grinding rivets3.JPG (57612 bytes) Grinding rivets4.JPG (52064 bytes)

The angle grinder gets the rivet heads down flat with the shoe.

8

Drilling_rivets_1.JPG (62118 bytes) Drilling_rivets_2.JPG (79333 bytes) Rivet_pounded_out.JPG (86510 bytes) First_rivet_removed.JPG (59308 bytes) Rudder_shoe_screw.JPG (61575 bytes)

The 1/2" drill bit makes short work if what's left of the rivet heads and a hammer and punch knock the rivets out the other side. The only problem here was a large wood screw on the leading edge of the shoe that was hidden by old bottom paint. Once it was removed, the rudder shoe dropped off and we dropped the rudder from the bottom of No Worries.

9

Rudder shoe1.JPG (108661 bytes) Rudder shoe 2.JPG (47011 bytes) Rudder shoe 3.JPG (43572 bytes) Rudder_shoe_scraping.JPG (66165 bytes) Rudder shoe.JPG (80814 bytes)

The rudder post shoe is a very nice looking piece of hardware and is in great shape after a little cleaning it's ready to go back on.

10

Rudder.JPG (50036 bytes) Rudder cleanup.JPG (71637 bytes) Top of rudder 1.JPG (86425 bytes) Top of rudder 2.JPG (58266 bytes) Bottom_of_rudder_1.JPG (69897 bytes) Bottom_of_rudder_2.JPG (86664 bytes) Cleaning_rudder_shoe_mounting_area.JPG (54627 bytes)

The rudder is cleaned and prepped while sitting on the concrete and Ana cleans the rudder skeg.

11

Thruhull_for_rudder_post_5.JPG (75242 bytes) Rudder_post_hull_hole.JPG (90377 bytes) Thruhull_for_rudder_post_1.JPG (52334 bytes) Thruhull_for_rudder_post_2.JPG (45650 bytes) Thruhull_for_rudder_post_3.JPG (62388 bytes) Thruhull_for_rudder_post_4.JPG (54224 bytes)

Once we dropped the rudder, another problem showed up. It first appeared that there was quite a bit of damage and rot where the stuffing box pipe comes through the hull. After chipping away a little glass, it was apparent that the boatbuilder had filled the cavity with some type of foam that had eroded away.

12

Rudder_hole_faired_1.JPG (39913 bytes) Rudder_hole_ready_for_thruhull.JPG (32580 bytes) Rudder_packing_gland_with_5200.JPG (41254 bytes) Rudder_post_thruhull_-_finished_repair.JPG (42422 bytes)

I was able to clean the area out pretty well and filled it with epoxy. Then I used 5200 around the stuffing box pipe and attached the stuffing box back onto the inside of the hull. Looks like a pretty good seal this time.

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Rudder_hole_epoxied.JPG (77994 bytes) Rudder_hole_faired.JPG (54999 bytes) Rudder_hole_leveled_and_ready_for_thruhull.JPG (60075 bytes) Rudder_post_stuffing_box_set_in.JPG (82479 bytes)

The mounting surface for the stuffing box was epoxied and sanded. Lag bolts were used instead of studs. Decided to turn the box 45 degrees so the lag bolts could bite into new wood.

14

Ready_to_put_back_in_the_water_3.jpg (38657 bytes) Rudder_getting_hooked_back_up.JPG (39074 bytes)

Put new zinc on the rudder and reattach the steering and autopilot and the job is complete.